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B-2018-1590Testing Engineers, Inc. �. Quality Assurance Services Materials Consulting 1 Since 1954 Regular Concrete Compression Test Report Project No.: 69029 Client: APP337 Sample No.: 261050 / Page 1 of 1 Project Name: Report Date : 08/16/19 10500 DeAnza Blvd. Sample Date: 07/19/19 DA03 Pit In -Fill Time Sampled: 0715AM Cupertino, CA Date Received : 07/25/19 Permit # B2018-1590 Inspector: E. Ledezma, TEI Supplier: Central Concrete Mix: 608 Ticket No.: 18871941 Location: Plumbing and electrical trench repair. Specimens Cast (ASTM C-31) : 5 Air Temperature (ASTM C-1064) : 58 deg F Mixture Temperature (ASTM C-1064) : 70 deg F Slump (ASTM C-143) : 4-3/4 inches Capping Specimens _ ASTM C-617 ASTM C-1231 Date Tested 07/26/19 08/16/19 08/16/19 08/16/19 HOLD ID Number, 3A 313 3C 3D 3E Mark Sample Dimension, Inches Diameter 4 4 4 4 Length 8 8 8 8 Area, sq. inches 12.57 12.57 12.57 12.57 Ultimate Load, Ibs 36670 57240 59490 58380 Ultimate Str., psi 2920 4550 4730 4640 Average, Str., psi 4640 Age Tested, Days 7 28 28 28 HOLD Fracture Type 3 5 4 5 Dry Unit Weight, pcf Specified Strength, psi 3000 3000 3000 SPECIMENS NOT SCHEDULED FOR TESTING WILL BE DISCARDED AFTER 28 DAYS OLD The Material /< WAS WAS NOT The Material Tested MET DID NOT MEET THE SAMPLED AND TESTED IN ACCORDANCE WITH THE REQUIREMENTS OF THE BLDG. DEPT. OR DSA APPROVED DOCUMENTS. REQUIREMENTS OF THE BLDG. DEPT. OR DSA APPROVED DOCUMENTS. Remarks: Samples Tested in General Conformance with ASTM C-39 1 cc. City of Cupertino 1 cc. Apple Computer Inc. Reviewed By: Robert Green Concrete Lab Supervisor The results presented in this report relate only to the item(s) tested. This report can be reproduced only in its entirety unless written permission from TEI is obtained. Corporate Office - 2811 Teagarden Street, San Leandro, California 94577 - (510) 835-3142 - Fax (510) 834-3777